I stumbled on some motion activated LED bulbs on Ebay from China and thought it would be a good solution to my motion wall mount porch light that had died. A replacement was around $40 from Home Depot and it didn’t match my existing lights.
While waiting for the bulb, the listing got removed. I became curious about the reason and guessed that the bulbs were not UL/CSA/EU safety certified. Though the risk is small since the bulbs are low power, if they did start a fire, your house insurance may not cover the damage.
When the bulb arrived, I didn’t notice any safety certifications on the box and will probably not use it. I tested it and it did seem to work. It was a bit longer than a typical bulb and so it didn’t fit my light fixture.
Just a precaution for those ordering electrical products on Ebay from China.
I posted about a temporary fix to a non-booting HP G56 laptop here by wrapping it in a blanket. After fixing a PS3 by baking the motherboard (see post here), I was confident in using this technique to repair the laptop.
First step was to disassemble the laptop. I removed the battery, the bottom access panels, the RAM memory, the wifi adapter, the hard drive and all the screws. I was then stuck and consulted this video on youtube.
The next step was to remove the keyboard. I had trouble removing the keyboard and it ended up being a few screws I had missed from the bottom including one underneath an access panel. I ended up breaking one of the key caps as well which I carefully crazy glued back on. There are four tabs on the bottom of the keyboard so you need to pry up from the top.
Once the keyboard was out, the case could be snapped opened to access the motherboard. I removed the fan, the socket-mounted processor (turn the screw 180 degrees to release) and the battery since these could not be put in the oven with the board.
I prepped the board with standoffs, insulated the electrolytic caps and applied some flux to the BGA video chip. I then baked in a preheated 375 deg F oven for six minutes like the PS3 board.
Once the board cooled, I put everything back together and the laptop booted up no problem.
Update: The laptop is flaky again after a couple of months though the blanket trick will bring it back up.
I got hold of a broken PS3 that wouldn’t power on. When you hit the power button, the yellow light flashes briefly, the system beeps three times and then it shuts down. This symptom is defined as the yellow light of death (ylod). The Xbox also has a failure producing a red ring of death (rrod). Having researched a similar problem with a HP laptop, see post here, I knew the issue was probably flaky lead-free solder ball connections under BGA (ball grid array) chips.
I found a good guide on taking apart the PS3 here. The rest of the guide attempts the repair with a heat gun. The problem with this approach is that applying heat to one area could warp and stress the board. I then read a few guides whose repair method was to bake the board in the oven. Though this guide here had lots of detail, I didn’t like the technique of turning on the oven with the board inside. This could potentially burn the board. If you’ve ever tried to bake cookies as a kid without pre-heating the oven, you will know the result.
I disassembled the PS3 following the first guide. You need a security Torx T10 screwdriver to remove the cover but my regular Torx T10 worked. You may be able to remove a security torx with a small flat screwdriver if you don’t have the right screwdriver. The guide was pretty helpful though I took the power supply off earlier in the process since it was restricting access to a ground wire.
It appeared my PS3 had been taken apart and repasted before since the thermal paste was not dried up and a few screws were missing. Repasting will not fix this problem but should be done if your PS3 still works but is running hot as a preventative measure.
Following some tips, I prepped the board by insulating the electrolytic caps with Instant TAC (dollar store) but I didn’t use small pieces of tinfoil on them since I figured it would just draw heat to the area.
Once you have the thermal paste off, the two big chips actually have heat spreaders on top of the actual ICs. These can be removed to replace the small bit of paste underneath but I didn’t bother.
I also didn’t prebake the board at low temperature in the oven and only used a bit of flux I had leftover in a pen. It was difficult to get flux underneath the chip but it’s probably not too crucial of a step.
I used bolts I had lying around to make standoffs to raise the board up. I was short nuts but these can be bulk purchased at Home Depot for 20 cents each.
For thermal paste, I used ceramic based compound instead of the recommended AS5. AS5 is conductive and spillover might cause a short. Since my board had been repasted, it wasn’t too difficult to remove the existing thermal paste.
Following this guide, I preheated the oven to 375 deg F. Melting point for lead-free solder should be around 360 deg F.
I put the board on a cookie sheet lined with aluminum foil and baked for 6 minutes. I then shut off the oven and opened the door. I didn’t bother using fans to cool the oven.
After the board had cooled, I reinstalling the board and the PS3 powered up. With this success, I wanted to bake my friend’s G56 HP laptop which will be covered in a future post.
I updated the firmware to the latest but shouldn’t have done that step. Firmware versions 3.55 or earlier can be jailbroken.
Since the PS3 didn’t come with any controllers, I had a difficult time finding used ones since they are heavily in demand. I did find a solution by using wired PS2 controllers than can be plugged into a PS3 with a USB adapter that can be found on ebay. I ordered one a bit too soon since there are dual versions that accept two controllers on one USB plug. PS3 controllers are also heavily counterfeited and new ones on ebay might not be genuine.
Edit: The problem with using PS2 controllers with the PS3 is that the PS2 controllers do not have a PS button. This button is used to connect to the console, check battery level, exit from a game to the main menu and holding it down will give an option to shut off the console. Also some games don’t seem to work like Gran Turismo 5.
Edit: After a couple of months of little used, the YLOD has come back. Not really worth rebaking since I got hold of a slim with a bad DVD drive but the DVD drive and hard drive could be salvaged from the fat PS3.
I had updated my front door knob and deadbolt to Kwikset Smartkey and wanted to change the knob on my shed to Smartkey so I could use the same key. I had installed a cheap Defiant lock and over the years, the base was cracked and the knob tarnished. The cheapest Smartkey lock was the Kwikset Tylo Satin Chrome available by mail order on Home Depot’s US website for $16 USD. However, when I installed it, the cylinder was upside down. The slot should be at the bottom and the key should be inserted with the teeth facing down. I checked the instructions and they indicated it was ok to install it that way. I googled the problem later and found out the cylinder could be flipped. The official way is to use a special tool but there are some youtube videos on how to flip it without the special tool.
The cyclinder is held in by two spring clips that need to be pushed in to release it from the knob. The access is very narrow and it is difficult to see the ends of the clip. What worked for me was to use needle nose pliers to push in a sliding tab at the opening to better access one side of the clip. I pushed a small hex key in there to push out one side of the clip. I could then use a small screwdriver to release the more accessible side.
Full model number is LN46A530P1FXZC. I fixed the same model previously with a washed out screen by replacing the TCON board here. This one had trouble turning on. Checking the power supply board, I found two bulging caps. Both had values of 1000uf/10V. I replaced them with 1000uf/16V (just slightly taller) and the TV powered up fine.
As part of my basement reno, I needed a solution for the bathroom door that swung inside a small bathroom. With the limited space, a pocket door would be ideal but would require reframing the opening.
I found a solution in the Johnson 2610F Wall Mount rail kit which converts any door into a externally mounted sliding door. I bought the 7ft version on Ebay . The longer length can be cut down with a hacksaw.
The important dimension is the door should be at least 1-1/4″ wider than the opening. I used the existing door though it is a little bit too narrow which meant the door could come off the bottom plastic guide when closed. The length of the track should be at least double the width of the door.
Installation is pretty straight forward and they have a video on youtube.
I was able to get inset handles that fit the existing knob holes and i plugged the latch hole with a cut piece of wooden broom handle. The hinge mortises I filled with cut ends of a 2×4 which was close to the hinge dimension.
Since I have fairly thick molding around the door, there was a bit of a gap between the door and the frame so I added weatherstripping to the inside frame.
For a privacy lock, I installed a sliding latch on the inside frame with the bolt extending into the door when closed. In an emergency, the door could be opened by removing the screws in the plastic guide rail at the bottom and tilting the bottom of the door out.
During the reno of my basement, I heard a loud buzzing coming from a bedroom and I suspected it was the doorbell transformer. Since they are typically mounted to an electrical box for AC power, I disassembled the ceiling light and found two wires coming from a knockout on the top of the ceiling box. I disconnected the wires and the buzzing stopped but my front door bell was also dead. I determined I would have to cut out the drywall to repair or replace the transformer and since I planned on painting the ceiling, there wasn’t a reason not to fix it. Cutting a hole large enough to access, I took a pic with my cell phone to determine how the transformer was mounted. A screw was expanding a collar connecting the bottom of the transformer to the ceiling box. Once I had the transformer out, I could see the problem. It looked like when it was originally installed, it was missing a rivet at the top holding the plates together. The installer just put a nail into the hole and bent it to hold it together. I headed to Home Depot to buy a bulk nut and bolt for around $1, fixed the transformer, reinstalled it, and patched the ceiling.
My car alarm wasn’t arming one day and I realized that the passenger side door wasn’t locking with the key fob. Once I manually locked the door, the system would chirp and arm. It was obvious the power door actuator had failed. Searching for the part on online part stores gave me a part number which I could then comparison shop. There were lots of non-OEM parts on ebay for less than $10 USD and the cheapest original Honda version was around $55. There could be a huge profit potential in counterfeit parts by putting a fake Honda sticker on the cheaper part. The ebay seller I ended up buying from, hondapartshub, was a Honda dealer with an online parts store. The same actuators are used in model years 2002-2006 for the RSX and in other Honda models like the Odyssey.
I found a guide to replace the actuator here but it was missing a few tips and steps. You have to remove the door panel first which is fairly easy. Once you removed the handle, power window switch and the 3 screws, you can easily pop the door panel off from the bottom and lift it up without any special tools.
With the actuator, you need to disconnect two rods to be able to pull out the assembly. The gold coloured rod needs some pressure to release it (use pliers or pry with a screwdriver) but it will come out. If you don’t disconnect it, you will end up bending the rod that goes up to the top of the door.
I also had some problem with the three screws at the edge of the door holding the latch. You need a #3 phillips (with a flatter tip). A normal phillips bit could strip the screw head.
To get at the latch, you will also need to remove a 10mm bolt that holds a guide rail for the window.
My last mistake was to not remove the protective cap on the new actuator before installing it since there is a small clip that holds it in place.
The same day I replaced my passenger side acutator, the driver’s side failed. The part for the driver’s side I ordered from a different ebay seller. My original replacement was in a bubble wrap bag with a Honda sticker and one of the terminals capped. The replacement for the driver’s side came in a box with a sticker, no bag and no cap though the ebay picture showed the part in a bubble wrap bag. I am a bit worried that it was counterfeit but have no way of knowing for sure. That seller’s store sells a lot of Honda parts.
Edit: My friend’s Acura had failed actuators and I purchased a non-OEM set (right and left) for him on ebay for $20USD and helped him install. Seems to have no issues with them so far.
Update: My friend’s $20 actuator failed on one side. It was also blowing the fuse as well. So wouldn’t recommend the cheaper replacements.
My brown 60’s bathtub was in need of a replacement. The problem I had was mainly the colour of the tub and some rust on the outside lip. The grout had a bit of mildew in spots and I was worried it was coming from behind the wall. The ugly floral tiles and seashell soap holder tile also needed to come down.
I had replaced the shower valve with a pressure balanced one previously (no more blasts of hot water when someone turned on a faucet or flushed a toilet. See post here. The next step was to replace the bathtub (before the floor and vanity).
To minimize plumbing, I wanted a replacement bathtub close to the height and drain location close to my existing tub. Most tubs carried in big box stores are “above floor drain”. These tubs are higher to allow the drain pipe to run above the floor where the floor can’t be cut out such as in concrete condos. The only model I could find close to my original tub was the Bootz Aloha carried at Home Depot in the US. The Canadian version was an above floor model. Thinking I would need to rent or borrow a truck to bring it back, I measured the box and determined it would just fit into my hatchback so my first hurdle was solved.
I had looked into bathtub reglazing and research indicated it only lasts about 5 yrs. I did find an epoxy painting product but for both, the cost would almost be the same as a new tub.
The next design challenge was choosing a backerboard. The best and most economical solution I found was Densshield which is a drywall product coated with a waterproof layer. I did my research and read and watched a few installation videos on youtube.
One feature I did want to add was a shower niche. I looked at buying a pre-built niche and ended up building one with 2×4’s and densshield.
With densshield, the face is waterproof but the edges are not. In their videos and instructions, they recommend using polyurethane sealant or silicone to seal joints. I picked up Sikaflex sealant from Home Depot for this application since thinset would more easily adhere to this.
For the tiles, I wanted something that wouldn’t look dated in 10 yrs. Though larger tiles are more modern, subway tiles tend to be timeless. I settled on 6×8 tiles and 2×2 green glass tiles inset in a diamond pattern for a small design feature. I purchased these at Lowes since they are sold individually there.
Step 1 – Demolition
My friend came over to give me a hand with the demo and tub installation. Hammering out the tile, the area behind the tub was dry and mold free.
To remove the tub, the drain had to be unscrewed out. I had purchased a drain wrench but it wasn’t really needed and a pair of slip-joint pliers could be used by sticking the pliers inside the drain.
With the tub removed, there was a bit of a time capsule in garbage the original installers left inside the old tub cavity. There was an old pepsi bottle, boxes from some of the bathroom accessories and leftover mosaic tile from the original walls. I considered using some of the original tiles in my design but couldn’t really fit it in.
I took the old 60lb steel tub to the metal recyclers and got a whopping $2 for it.
Step 2 – Tub Installation
The drain pipes in my 60’s house were 1-1/2″ copper using compression fittings for the tub drain. When we dry fit the tub, the drain location was about 1/2″ off and we were able to line it up by angling the drain pipe. The overflow pipe was too long so I cut it down and used a Fernco fitting to reattach it which also gave it some play to line up properly. The shower valve also no longer lined up to the center of the new tub but it could easily be moved since the copper pipes have a bit of play when not attached to the framing.
When I replaced the drain, I didn’t tighten it enough nor did I check it adequately for leaks so I had to replace some wet drywall on the ceiling downstairs.
There is a good youtube video on installing the Bootz tub from the manufacturer though they don’t recommend any product names.
Step 3 – Framing the niche
With 6×8 tile, I wanted the niche to fit four of these inside so I made the niche 12×16 which could hold several soap and shampoo bottles. A minor problem arose since an electrical cable ran in the area where the niche was going to be built. Luckily, there was enough slack in the wire after some clips were removed for the wire to go around the niche. I had to be careful with the measurements since I wanted a full tile at the bottom edge of the niche and it had to be centered.
Step 4 – Installing the Densshield
I picked up the Densshield at Lowes and it comes in 60″ x 32″ sheets which is perfect for surrounding a 5ft tub. However, I needed a little bit extra for the sides of the niche and the area beside the bottom of a tub. You should get a 4″ x 32″ strip left over with the two sheets on the main wall. Instead of buying and wasting an extra sheet, I cut strips from the top of the sheet opposite the shower head. This area would be the driest and would rarely be in contact with water.
One question was how to install the Densshield over the bathtub lip. I left a 1/8″ gap (spaced with a nail) and also used 2×4 blocking where possible to give both the lip and Densshield and edge. In hindsight, I should have used a minimal gap like 1/16″ since it is hard to fill a larger gap with the sealant.
For screws, a box of 200 1-1/4″ Rock-On backerboard screws was enough for this project. Screws were set every 6″ following the instructions since it has to hold a lot of weight with the tile.
I put Sikaflex between the butted joint on the wall, the inside corner joints, over the screw heads, and the exposed edge of the Densshield along the bathtub lip. I also sealed all the pipe openings and the edges when I lined the niche with Densshield. There are youtube videos where they use a paint-on waterproofing membrane like Aquadefense or Redguard on the edges but those are not available in small quantities and Sikaflex should work just as good. The Sikaflex does take a couple days to cure so I covered the walls with dollar store shower curtains since I needed to use the shower while it dried.
After it was dry, I reinforced the joints with cement board tape and modified thinset.
There is also a good youtube video from the makers of Densshield on the installation process.
Step 5 – Tiling
My existing tile wall is about 64″ high above the tub. With 6×8 tile, I would need 10 and half rows of tile. I had used the following:
4 sheets 5′ x 32″ Densshield (Lowes)
Pack of 200 1 1/4″ Rock-On cement board screws
2 tubes of Sikaflex polyurethane sealant (Home Depot)
Fibatape cement board tape
140 pieces 6×8 tile (Lowes sold by piece)
20 pieces 6×6 tile (Lowes sold by piece)
4 – 2″ x 2″ green glass tile (Home Depot)
50lb modified thinset (I had about 5 lbs left over)
2 – 1lb unsanded grout (I had a leftover tub)
PVC 5/16″ edge trim (Schluter BW80)
1/4″ x 1/4″ notched trowel
budget grout float
mixer paddle attachment for drill (didn’t buy one but it would have been much easier than mixing thinset by hand) (Harbor Freight?)
The tile count is for 10 rows x 4 for each side wall and x 6 for the front wall with the ends using 6×6 tile. The 10 rows didn’t quite reach the old tile height so I added a row of tiles cut in half so I needed an additional 7 – 6×8 and 2 – 6×6.
I got lucky and found a used tile saw on craigslist for $20. I did want to buy a used one since I wanted to take my time and not be rushed with a rental saw.
For a decorative feature, I bought some square 2″ glass tiles and would embed these in a few corners in a diamond pattern.
The first row is the most important and needs to be level. Don’t count on your tub being level. You do want the widest gap to be minimal since it has to be covered with a bead of caulking.
I had originally bought tile adhesive which had indicated it was good for wet areas. After some online research, I returned it and switched to using modified thinset.
For caulking, it is recommended to use 100% silicone with mildew protection for bathrooms. I used GE Silicon II which has a short handling time.
I took my time and tiled over several days. For spacing, I used the nubs built into the tile instead of tile spacers. With both the densshield and sikaflex, I knew my walls were waterproof behind the tile.
To cut the tile for the openings, I used both a circular tile cutter I purchased at Harbor Freight and the tile saw. Since the wall was not perfectly plumb, I did a lot more tile cutting than I had originally planned.
Step 6 – Grouting
I had some leftover grout and the online MAPEI grout calculator indicated I should have enough with an extra 1 lb.
Grouting is pretty basic but a little tedious so I worked in sections. I also wanted to make sure the colour matched my tile when it dried.
I did contemplate sealing the grout but didn’t do this extra step.
Step 7 – New Shower Door
One thing I didn’t want was an ugly shower curtain with my new bathtub and tile walls. I was looking into a glass screen but found a modern, frameless sliding shower door at a local importer of Chinese made building products. The door is thick 8mm tempered glass but instructions were minimal other than an autocad drawing.
I installed the fixed glass panel first determining the position with the plastic guide that installed in the middle of the tub wall. Though the instructions were to screw it in place for an acrylic tub, I just siliconed it in place. From the position of the panel, I could mount the edge frame and screw it into the wall. Holes were easily drilled into the tile with a new masonry bit and some tape on the tile to minimize the bit from wandering.
With the fixed panel in place, I could then install the top rail since it is attached to the fixed glass panel. The allen key for set screws for the rail supports were not included but luckily I had a correct metric key in my tool box.
This LG 37LC7D had power issues and wouldn’t turn on. The usual suspects were going to be bad capacitors on the power supply board. Inspecting the power supply board found four bulged capacitors. 3 x 2200uF/10V (C202, C206, C217) and 1000uf/35V (C210 – may be 1500uF). After replacement, the TV powered up with no issues.
Edit: I have an encountered a second TV model with power issues. C202, C217 and C221 had been replaced but with wrong values. I would recommend replacing the following capacitors.
C202, C206, C217, C218 – 2200uF/10V
C208 – 2200uF/25V
C210 – 1500uF/35V
C221 – 470uF/10V
C222 – 470uF/25V
C226 – 470uF/35V
Update 2: One of the TVs came back with an issue of shutting down by itself. I replaced the main board and it appears to be fixed.